This paper presents a model for resolving the problem of wasted time in the production of atypical factories. The use of modern technology in the machinery within the production lines, training workers to raise their performance and how the production line design leads to an increase in the amount of production are the most important factors to solve that problem. Specialized machinery was used in the production line "T-shirt", the efficiency indicators were considered and the productivity standards were used by balancing production lines inside the sewing halls, the workers' performance got raised through training on a variety of production stages, their performance was observed in the implementation of processes within production lines and operation time for each stage has been calculated. The number of manpower used in production lines has been reduced along with the operating time for the piece of clothing as shown by this research results. The research was conducted through several stages:
Analysis: The sample was analyzed and the current situation of the factory of this study was described.
Goal-setting: A range of targets including taking advantage of the possibilities of factory workers, machines and tools has been set.
Design for the proposed production line: The aim is to producing design for T-shirt production line with reducing the operating time.
Testing and evaluation of the proposed system through results: The results reached shows how the design of production lines affects can reduce operating time with different product forms, as the factory gives atypical production, sewing production rates increased and the product operating time decreased.
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